OK, Here is what I have:
I just re-installed my 727 after a home rebuild. I seem to have lost my high-gear. Low engages smoothly and when I shift to second, it also engages smoothly. Nothing happens when I shift into high. No noises or anything either. During the rebuild, I also dropped in a new converter. It isn't the linkage or the kickdown band adjustment. After some more testing with it on stands, I don't appear to have any "auto" function at all. I get manual first and second, but no drive. Drive seems to put it right into second. After looking though the FSM, I pulled the tailshaft to check the governer - moves freely. I did recheck the kickdown linkage before tearing into anything - no pressure on the arm at idle. BTW, do I need to have a return-tye spring hooked up? Never had one, but wondering if I should.
Dropped the pan, and didn't find great news in there, but I would like some opinions. Pictures are attached below. I believe the junk is left-over from my torque converter failure - what caused the rebuild in the first place. I am guessing that this is what was left in the cooler - I thought I had it all cleaned out but I guess not. I installed an in-line filter (PH-8A), but forgot to hook it up when I first started it. Subsequent tests and run-ups were done with it hooked up. Could my trouble have been caused by inadequte fluid flow? I am thinking that with this stuff in the pan, the in-line filter is probably plugged with crap as well. I will be opening the VB tonight to make sure I put all the check balls back in the right spot. Thoughts?