The car went to the paint shop today. This was the first sunlight the car had seen in several years. Replacing lots of metal, new includes: R/T hood, trunk lid w/ spoiler holes, both rear quarters (full), and roof skin. Expect 3-4 months, will pay in increments to cover work completed at each step (suggested by autobody101 website). The body shop really liked the idea.
Sealed the seams with 3M ultrapro urethane seam sealer (not firm and fast) per suggestion of the website mentioned. The body shop said they use it also, and liked the way it turned out on the Challenger. I'm adding the headlite buckets to adapt 1970 grille to the 74.
Now for a drive train update. I already rebuilt the rear axle/rear diff. I did NOT use "green" wheel bearings, I stayed with the semi-floating tapered Timken bearings because they support side load (turning corners), and the green ones do not. For the pumkin used 742 case with clutch type posi (sorry, I've always called them that). I like the case because there is no crush sleeve, its all shims for bearing adjustment. I liked the clutch posi because it is rebuildable. I had originally picked up a cone-type posi. Being the ex-ASE certified mechanic that I am, I have to tear everything apart. Well.... the cone type unit was in usable shape true to what the seller said, but there were "hard areas" in the case casting, which were causing gaulling of the cones. So I could see the unit would not last long term. I cut 0.080 off the ends of each cone to extend the life of the unit as recommended in "Chrysler Performance Upgrades" by F. Adkins. I then sold the pumkin.
The 742 unit I have has a flat and true ring gear case, I replaced all bearings, and added NEW OEM ring and pinion 3.23 ratio. Hard to find this ratio, but an outfit in Long Island had several.
The trany was another story. Looked at the trany before buying, it turned over ok, but a little stiffness in spots. I thought, ohh, I can fix whatever it is. WELL..... the previous builder had left out one of the spacer/washers that supports the end of the double set of needle bearings at the end of the counter shaft . So the needles were feeding into the groove in the case that retains the thrust washer. The needles were being eaten alive by the case, and vice verse. The case and countershaft gear were ruined.
So I bought a used case and bearings/rebuild kit from Brewer's Performance, he's a great guy to deal with. I bought a complete set of gears from Zumbro Bearing and Gear (ZBAG) in MN, they were also very helpful. The gear set was not OEM, and they said it would not hold up to 600 hp 6000 rpm clutch dumps with slicks, but I"m not going to race the car.
So in the end the used trany had a good input shaft bearing retainer, and the better shift cover assy (the good early style). I replaced all the bearings, new countershaft and an OEM new output shaft and syncro assemblies. Also new steel shift forks from Passion Performance.
The gear set I bought has the "older" lower first gear ratio (2.66:1) so when it's combined with a 3.23 axle ratio gives you 8.59:1, which is real close to the newer first gear ratio (2.47:1) combined with a 3.55 axle ratio (result = 8.77:1). SO... I have the low first gear for good acceleration, and also have a highway type rear axle ratio. Trying for the best of both worlds. Should work well I think.
I had the bell housing opening enlarged to fit the large diameter front bearing retainer.
Does money grow on trees??? I wish it were true. I'll be returning to working on the cylinder heads next; they are half done. Port molds, pushrod restrictions, more lessons learned.