Those additives go against everything I believe in, which is do it right. However my mechanic friend told me it might get me soe more time until I had the money for a new engine.
It didn't smoke at all before the restore, however I do not think that has anything to do with it.
If this motor comes out it's not going back in. With the end of the crank ground up, the fact it's a 318 with 150,000 miles, broken off valve cover bolt, I do not think it's worthwhile to put it back in or spend another dime on it.
In the meantime I will go a leakdown test and see what happens. My buddy has the tools to replace the valve guide seals so I may do that as well.