Ok so it ran like a bat out of hell when it was dynoed so I don't believe the 650 D P is too big but here is where I am as of today. took the plugs out and they were black from too much fuel (smelled like gas and they had a hint of liquid residue on them) and gapped at .28. I cleaned them up and gapped them to .35. I also put in a fuel pressure regulator and set it at 5 1/2. Fuel pump puts out 7. I then started it up and ran better than it has since I got it running in the car. However, it backfired thru the exhaust one time when I revved it up to 4,000rpm's and the secondaries kicked in but it sounded smooth and clean and until I hit 4,000rpm it sounded better than ever. I immediately shut it down because I didn't want to have my plugs dirty again. I think I need to rejet the primaries down two sizes and see if that helps but if it ran so good during the dyno , could it be that having it in the car with the drive train and car weight it is running rich because it is not as free running as the drag of waterbrake would put on it and now its not since its pulling actual weight drive train and all? HELP! I've got until Monday to get it roght because I have to take off to N.C. for my grand opening show and GOLDEN COMMANDOS induction to the East Coast Drag Times Hall of Fame. Oh and it is a 273 Commando LA block registering 381 HP AT 6,500 rpm. The cam has .517 lift and 296 duration.